Case Studies

SCORPION™ COMPOSITE PLUG CASE STUDY

Read the story of how over 100 Scorpion™ Composite Plugs were milled out using only 1 bit.

FLOWGUN™ CASE STUDY

Actual pressure test results that showcase the effectiveness of FlowGun.

WIRELINE CASE STUDY

On target to save operator in the Permian approximately $300,000 by year end.

RAPID SET 1 CASE STUDY

WOC times reduced to less than 8 hours, saving approximately 8,000 in NPT per well.

Coiled Tubing Case Study

An operator in Haynesville saved more than 55 days and $4 Million with unique high pressure coiled tubing fishing technique.

BREAKTHRU™ CASE STUDY

Nine helped a customer land 17,000 feet of casing across a 9,000-foot lateral and boost recovery revenues.

LONG RANGE SERIES™ (GEN 1) WHITEPAPER

Read more about how the Long Range (Gen 1) can overcome compromised casing in long laterals.

LONG RANGE SERIES™ (GEN 1) WHITEPAPER

Unique solution to repair casing failure in a HTHP wellbore allows for successful multi-stage stimulation treatment in an unconventional reservoir.

LONG RANGE SERIES™ (GEN 1) WHITEPAPER

Solid expandable liner system with custom composite frac plugs enable recovery of lost reserves in the Piceance Basin

eBooks

OVERCOME CASING INTEGRITY ISSUES E-BOOK

Discover how the Scorpion Extended-Range Plug can help solve casing-integrity issues in complex horizontal wells.

ACHIEVE REQUIRED TOC IN DEPLETED ZONES E-BOOK

Learn more about how to achieve optimal top of cement in depleted zones such as the Permian.